Message-ID: <5387955.1075854133624.JavaMail.evans@thyme> Date: Thu, 15 Jun 2000 04:18:00 -0700 (PDT) From: gary.hanks@enron.com To: cheryl.dudley@enron.com, pat.clynes@enron.com, daren.farmer@enron.com, shawna.flynn@enron.com, james.mckay@enron.com Subject: Shut-in of #986315 Mime-Version: 1.0 Content-Type: text/plain; charset=us-ascii Content-Transfer-Encoding: 7bit X-From: Gary A Hanks X-To: Cheryl Dudley, Pat Clynes, Daren J Farmer, Shawna Flynn, James McKay X-cc: X-bcc: X-Folder: \Darren_Farmer_Dec2000\Notes Folders\Logistics X-Origin: Farmer-D X-FileName: dfarmer.nsf Meter 0986315 Shawnee Spring Common Point was shut-in on 6/13/2000 due to high dew point. Repeated attempts by the pumper to dry out the gas have failed. The meter will remain shut-in until the dew point is within pipeline quality specs. Gary H. ---------------------- Forwarded by Gary A Hanks/HOU/ECT on 06/15/2000 10:47 AM --------------------------- From: Sean J Smith 06/14/2000 05:55 PM To: Gary A Hanks/HOU/ECT@ECT cc: Subject: #986315 I received a call from Carl Drachenberg with HMS at approximately 1:45 PM on 6/13/00 stating that he pulled a stick on meter #986315 and it was wet and flowing at 35 lb. I asked Gary Hanks what we want to do and he said to have Carl notify the producer and shut it in. I notified Carl and he got in touch with the producer and they shut the compressor down at approx. 2 PM on 6/13 and at that time there wasn't any flow. Carl came back out there at 8 AM on 6/14 and closed the valve and removed the chart. There was no flow after they shut the unit down and it was flowing between 500 and 300 mcf. The meter is now out of service. Any questions - you know where to find me.